I am not sure... More detail about the restoration here.
https://www.apres.org.uk/feature/the-peoples-mosquito/
I am not sure... More detail about the restoration here.
Just how thorough do y'all think a wartime BoI be?
I imagine a wartime board of inquiry might have been somewhat cursory but this accident occurred in 1949 and apparently technical changes were recommended to the Merlin 113/114 engines as a result. What those changes were I haven't a clue.
ian16th your insightful comment about the Merlin 113/114 engines and fuel reminded me that they were upgraded to work with 150 octane fuel. I wonder if this could have had something to do with this accident?
I didn't mention Merlins and fuel!TheGreenGoblin wrote: ↑Thu Apr 29, 2021 4:31 pmian16th your insightful comment about the Merlin 113/114 engines and fuel reminded me that they were upgraded to work with 150 octane fuel. I wonder if this could have had something to do with this accident?
Yes, you didn't! Your insight was a possible fuel system problem. Where did that notion come from? Ah yes, it was your mention of fuel systems that triggered a memory of reading about the octane upgrade for the Merlin 113/114 engines, read by me in the dim distant past. The Beverley non-return fuel valve fitting sounds like an unfortunate mistake to make. Sad ending for the puppy hounds.ian16th wrote: ↑Thu Apr 29, 2021 5:16 pmI didn't mention Merlins and fuel!TheGreenGoblin wrote: ↑Thu Apr 29, 2021 4:31 pmian16th your insightful comment about the Merlin 113/114 engines and fuel reminded me that they were upgraded to work with 150 octane fuel. I wonder if this could have had something to do with this accident?
The Beverley incident I referred to was none return valves fitted the wrong way. The incident made big news because a lot of Police Dogs, destined for Akrotiri, were killed!
The next Beverley to carry Police Dogs, was the one that I was on, for the leg Abingdon to Istres.
https://www.baaa-acro.com/crash/crash-b ... -20-killedTotal fatalities: 20
Circumstances: The aircraft departed RAF Abingdon at 1042LT bound for RAF Akrotiri in Cyprus. It was carrying cargo, a relief crew, eight RAF police dog handlers and eight police dogs. There was low cloud at 500 feet (150 m), visibility was less than 1,000 feet (300 m), and an easterly wind of 10 knots (19 km/h). As the aircraft climbed, the engine number one developed a fuel leak. The flight crew responded by shutting down the engine and feathering its propeller. The flight crew declared an emergency and requested a blind approach to RAF Abingdon. The controller alerted emergency services on the ground. A short time later, cockpit instruments alerted the flight crew to a large loss of fuel from No. 2 fuel tank, the second of four such tanks in the port wing. In an effort to stop the leak, the crew de-activated the fuel cocks and boosters for the No. 2 tank, but left them on for the No. 1 tank. As the Beverley turned on to final approach for RAF Abingdon the crew attempted to increase power from the remaining three Bristol Centaurus engines but No. 2 engine – also on the port wing – failed to respond and the aircraft began to lose speed and height. Knowing he could not reach the airfield, the captain tried to land in a field. However, the aircraft became uncontrollable and struck a number of high tension cables and a group of elm trees that tore the port wing from the fuselage. On impact with the ground, the aircraft destroyed a caravan and a prefabricated house before somersaulting and crashing upside down. Eighteen occupants were killed, among them three crew members, and two people on the ground.
Probable cause: A Board of Inquiry investigated the crash and found it was caused by loss of power from Nos. 1 and 2 engines, both mounted on the port wing. George Ward told the House of Commons that "the four fuel tanks on the port side of the Beverley feed into a collector box from which the two port engines are fed. From the available evidence, including inspections of part of the aircraft's fuel system, it is clear that a non-return valve between No. 1 (port) tank and the collector box had been fitted in reverse and that the fuel supply from Nos. 3 and 4 (port) tanks were switched off throughout the flight." Ward continued, saying that the loss of power from No. 1 was caused by it being shut down as a precautionary measure, and the fuel starvation to No. 2 engine was caused by an incorrectly fitted non-return valve in the supply line from No. 1 fuel tank. No. 2 fuel tank had been isolated and two smaller fuel tanks in the port wing had not been selected during the flight. The tradesman who had fitted the valve, and his supervisor, were prosecuted and charged, and the technician was court-martialled for negligence and punished with a reprimand. The Board also noted that some fuel was available from two smaller tanks but they were not used during the flight, and that the captain "must bear some responsibility" for not using those tanks. Ward said, however, that "owing to the nature of the flight the amount of fuel in the two smaller tanks was not large, and it can only be assumed that the captain had no reason to believe that both port engines would not operate satisfactorily off the two main port tanks individually." The captain was killed in the accident and no allegations were brought against him or any of his crew.
https://navywings.org.uk/sea-fury-t-20-update/Thursday 29 April
Firstly, and most importantly, one member of the aircrew has now been released home and the other aircrew member remained in hospital overnight as a precaution and will be released once Doctors are content. Both have been in contact with and seen by Navy Wings staff.
The site has been secured and visited by various agencies and once the AAIB have been on site tomorrow we will look to recover the aircraft. Plans are underway for that recovery.
We will be putting statements out on the website as we move through the various stages of recovery to keep you all informed.
Photographs herePilots Unhurt after Skilful Handling of Emergency Landing
Navy Wings Hawker Sea Fury T20 G-RNHF (VX281) was forced to conduct an emergency landing in a field close to RNAS Yeovilton earlier this week following a problem with the engine. Both pilots escaped injury but unfortunately the aircraft has been severely damaged.
The Sea Fury, which was on a routine training flight, suffered a significant drop in engine oil pressure shortly after taking-off and climbing away from the airfield. The pilots, both highly experienced former naval pilots, immediately carried out the appropriate drills and transmitted a PAN call.
They turned back and lined themselves up perfectly up for a precautionary landing on Runway 04. However, shortly before reaching the runway on close finals, the engine stopped, changing the speed and angle of glide of the approach dramatically, and they were forced to put the aircraft straight down into a field just outside the airfield boundary.
“The pilots’ skilful execution of an extremely hazardous situation was exemplary,” said Commodore Jock Alexander CEO of the Charity.
“We are all extremely relieved that they are safe and well. RNAS Yeovilton Air Traffic Control reacted immediately, and the Emergency Fire and Medical Services were very quickly on the scene. The support of the Air Station has been outstanding.”
The aircraft wings and engine detached during the impact and the fuselage rolled upside down but both pilots were able to escape unaided. They were taken to Yeovil hospital as a precautionary measure, and one was retained overnight for observation.
The Air Accident Investigation Branch (AAIB) and the Civil Aviation Authority (CAA) have been informed and investigations have begun into the causes of the accident.
“The Sea Fury is a classic and much-loved Fleet Air Arm aircraft, and the accident has been a shock to everyone in the Navy Wings community,” said Jock Alexander. “It is too early to say whether it is feasible to rebuild her and if she will ever fly again.”
The Charity’s Chief Engineer Jim Norris said “Great skill and calm was shown by everyone in the post-crash management team. We are grateful for the overwhelming support we have received. The aircraft will be recovered to the Navy Wings Heritage Hangar for the investigation.”
Although the Sea Fury T20 has been a favourite on the air show circuit, Navy Wings has worked hard in recent years to build greater resilience into the flying collection so that when the unexpected happens the Charity always has other aircraft that can continue to display to the public.
The Navy Wings collection also includes a Sea Fury single seat FB11, two Fairey Swordfish, the Sea Fury’s successor, a Sea Hawk and a growing number of other heritage aircraft, allowing these wonderful examples of our national aviation heritage to operate in the skies of the UK for many years to come.
TheGreenGoblin wrote: ↑Thu Apr 29, 2021 1:16 amIn this most recent accident they were very lucky that a fire didn't break out.